Friday, July 30, 2010

Transmission back out for repair




Well after filling the differential with fluid and then the trans, I found that the trans had a leak where the tailshaft bolts up to the main body. Never would have guess that but she had to come out and that's not any fun! So, off to the shop for gaskets and I figured while it's there get a full inspection of the internals. The mechanic said it looks like new inside and very low miles, so no rebuild needed. Gaskets won't be in until Monday so I'll have to wait.
I decided to get the front end aligned as close as possible while the trans is gone and I didn't like how that turned out. After taking the rack and pinion off several times to get the steering wheel centered and tires straight it sure seems like the subframe mounts for the rack are off to one side a half inch or more. I had to tighten one tie rod end up all the way and adjust the other to get it set. It's been a rough week as far as car progress goes. The enemy sure likes to find a weak spot and camp on it. This to shall pass!
I ordered a Diablo Program Tuner for the engine and it will be in next week.

Monday, July 26, 2010

Bumbed out today

The car was looking so good and having had it run was awesome. But the electrical was not right and after getting what seemed to be the best way to hook it up, turned out would not start the car. THEN there is a little issue of trans fluid on the floor. YES the trans is leaking and must be back pulled out. Not a happy camper!!!

Thursday, July 22, 2010

Starting to look like the old car again






















Well the short list is getting really short. The adjustable coilover shocks on the left side went on today and so I had to put the tires on for looks. Brake calipers, and new rotors for the front got mounted. All my electrical connections for startup are done but I had a blown fuse so it will be put off until tomorrow. Still have electrical questions on the table and I'm hoping I have most of them right. We'll see! Need prayers please!

Tuesday, July 13, 2010

Hoses and other stuff






















The Power Steering tank was going to be a clearance issue so I relocated it to the fender and it turned out well. I have the upper radiator hose on and used a chrome one as it shows and mostly because it can take the S curve needed to make it fit. The lower one I found on the back wall of Bennett Auto Supply and after moving the swaybar down with some spacers it fits great. The heater hoses make there way all around the engine bay to the far side where they go through the firewall. Again I had to hunt through the supply store to find ones I could make work with a little cutting and connecting. Still waiting on the new throttle body and the shock parts but they should be here this week. Then the wiring challenge! Urgh!!!

Kaye did some sewing for me as the shifter boot over the new Hurst 6 speed needed a little altering and she did a great job on that.

Thursday, July 8, 2010

Hood clearance issues










Well I got the front bumper installed and the new grill in place. I put the axles in and they were alot easier than I expected to setup.
The shocks came with the upper portion needing the original parts to install them-but-I had thrown the old ones out to make space months ago and now I'll need to go to Miata and order the replacement pieces. Oh well who knew!
Kaye gave me a hand to set the hood on and as I thought might happen I have some clearance issues to solve. The Ly6 throttle body is taller than a corvette style so I've order a replacement one and the P/S tank is to tall also. It's close but that what building a hot rod is all about. Being on an adventure in design.

Tuesday, July 6, 2010

LS Accessories bolted on




















Today it seemed like the adjustments went well and the only hitch is the new GM A/C unit will not fit in this space. I have the Miata unit so I'll have to make a bracket later on and use it. The radiator needed a little cut also the belt was touching the side wall at the alternator, so I was lucky that it could be knotched to fit.
The gauge cluster came out pretty easy after finding someone that posted his experience doing it on the net. Love that internet for info.
With the air intake on it looks pretty awesome. I'm working on a forced air ducting from the former roadlight hole in the bumper and up into the engine compartment where the filter sits.

Saturday, July 3, 2010

Motor and Trans mated back up











Well it feels good to have the problems taken care of and the engine and trans all mated up and the trans mount secured. I put the driveshaft in to make sure it was a fit and it's great.
The new bellhousing came from Arizona and only 2 dealerships had one. They quick shipped it for me and don't charge anything to do it. The shocks are scheduled to be here Monday and that pretty much does it for big parts stuff. Look at that new Hurst short throw shifter and I can't wait to put it in the console.
Happy 4th of July tomorrow

Thursday, July 1, 2010

Problems to solve






















Well after getting the engine in and checking her over i found a few clearance issues that were not acceptable. The rear corners of the block ar much to tight to the firewall and could cause a serious vibration during operation. The passenger header was up against the subframe and the collector could use a dent to give it more room. I also had an issue with the quick disconnect on the trans that required me to pull the trans back to make right. Well, in the process of doing the trans removal I cracked the bellhousing. OUCH!






So with a Mission trip to Nicaragua coming up on the 19th, I decided to let it sit and start the pullout and repair process when i got back. Igot sick when we returned and had to let this fever get under control before really geting back to the car.






I've cut all my wire ties that would restrick the motor being pulled up and forward and disconnected the others, like the exhaust maniflods etc. Don't really care for going backwards on this build but it will be a better car when these issues are fixed. Back to hooking up the lift and getting the motor mounts bolt out so it can go up and forward for the clearance work on the firewall I need.